battery INFINITI QX56 2004 Factory Service Manual
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![INFINITI QX56 2004 Factory Service Manual SE-40
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
DATA MONITOR
CAN DIAGNOSIS SUPPORT MONITOR
SELECTIOM FROM MEMU
Monitor item [UNIT] Contents
CAN COMM [OK/NG] When CAN communication circ INFINITI QX56 2004 Factory Service Manual SE-40
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
DATA MONITOR
CAN DIAGNOSIS SUPPORT MONITOR
SELECTIOM FROM MEMU
Monitor item [UNIT] Contents
CAN COMM [OK/NG] When CAN communication circ](/img/42/57034/w960_57034-2988.png)
SE-40
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
DATA MONITOR
CAN DIAGNOSIS SUPPORT MONITOR
SELECTIOM FROM MEMU
Monitor item [UNIT] Contents
CAN COMM [OK/NG] When CAN communication circuit is malfunctioning, it displays “NG”.
CAN CIRC 1 [OK/UNKWN]
Displays [OK/UNKWN] condition of the CAN communication judged by each sig-
nal input. CAN CIRC 2 [OK/UNKWN]
CAN CIRC 3 [OK/UNKWN]
CAN CIRC 4 [OK/UNKWN]
Monitor item [OPERATION or UNIT] Contents
SLIDE SW–FR “ON/OFF” ON/OFF status judged from the sliding switch (FR) signal is displayed.
SLIDE SW–RR “ON/OFF” ON/OFF status judged from the sliding switch (RR) signal is displayed.
RECLN SW–FR “ON/OFF” ON/OFF status judged from the reclining switch (FR) signal is displayed.
RECLN SW–RR “ON/OFF” ON/OFF status judged from the reclining switch (RR) signal is displayed.
LIFT FR SW–UP “ON/OFF” ON/OFF status judged from the FR lifter switch (UP) signal is displayed.
LIFT FR SW–DN “ON/OFF” ON/OFF status judged from the FR lifter switch (DOWN) signal is displayed.
LIFT RR SW–UP “ON/OFF” ON/OFF status judged from the RR lifter switch (UP) signal is displayed.
LIFT RR SW–DN “ON/OFF” ON/OFF status judged from the RR lifter switch (DOWN) signal is displayed.
MIR CON SW–UP “ON/OFF” ON/OFF status judged from the door mirror switch (UP) signal is displayed.
MIR CON SW–DN “ON/OFF” ON/OFF status judged from the door mirror switch (DOWN) signal is displayed.
MIR CON SW–RH “ON/OFF” ON/OFF status judged from the door mirror switch (RIGHT) signal is displayed.
MIR CON SW–LH “ON/OFF” ON/OFF status judged from the door mirror switch (LEFT) signal is displayed.
MIR CHNG SW–R “ON/OFF”ON/OFF status judged from the door mirror switch (switching to RIGHT) signal is
displayed.
MIR CHNG SW–L “ON/OFF”ON/OFF status judged from the door mirror switch (switching to LEFT) signal is
displayed.
SET SW “ON/OFF” ON/OFF status judged from the setting switch signal is displayed.
TILT SW-UP “ON/OFF” ON/OFF status judged from the tilt adjusting switch (UP) signal is displayed.
PEDAL SW-FR “ON/OFF” ON/OFF status judged from the pedal adjusting switch (FR) signal is displayed.
PEDAL SW-RR “ON/OFF” ON/OFF status judged from the pedal adjusting switch (RR) signal is displayed.
MEMORY SW1 “ON/OFF” ON/OFF status judged from the seat memory switch 1 signal is displayed.
MEMORY SW2 “ON/OFF” ON/OFF status judged from the seat memory switch 2 signal is displayed.
DETENT SW “ON/OFF”The selector lever position “OFF (P position) / ON (other than P position)” judged
from the park switch signal is displayed.
STARTER SW “ON/OFF”Ignition key switch ON (START, ON) /OFF (ignition switch IGN, ACC, or OFF)
status judged from the ignition switch signal is displayed.
SLIDE PULSE —Value (32768) when battery connects is as standard. If it moves BACKWARD, the
value increases. If it moves FORWARD, the value decreases.
RECLN PULSE —Value (32768) when battery connects is as standard. If it moves BACKWARD, the
value increases. If it moves FORWARD, the value decreases.
LIFT FR PULSE —Value (32768) when battery connects is as standard. If it moves DOWN, the value
increases. If it moves UP, the value decreases.
LIFT RR PULSE —Value (32768) when battery connects is as standard. If it moves DOWN, the value
increases. If it moves UP, the value decreases.
MIR/SEN RH R–L “V” Voltage output from RH door mirror sensor (LH/RH) is displayed.
MIR/SEN RH U–D “V” Voltage output from RH door mirror sensor (UP/DOWN) is displayed.
MIR/SEN LH R–L “V” Voltage output from LH door mirror sensor (LH/RH) is displayed.
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AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
3. CHECK SLIDING MOTOR CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect driver seat control unit and sliding motor LH.
3. Check continuity between driver seat control unit connector P3
terminals 35, 42 and sliding motor connector P4 terminals 4, 6.
4. Check continuity between driver seat control unit connector P3
terminals 35, 42 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and sliding motor LH.
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace sliding motor.
NG >> Replace driver seat control unit.
Reclining Motor LH Circuit InspectionEIS002YK
1. CHECK SEAT RECLINING MECHANISM
Check the following.
Operation malfunction caused by an interference with the center pillar or center console
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.35 (V/W) - 6 (V/W) : Continuity should exist.
42 (O/B) - 4 (O/B) : Continuity should exist.
35 (V/W) - Ground : Continuity should not exist.
42 (O/B) - Ground : Continuity should not exist.
LIIA0696E
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P335 (V/W)
GroundSliding switch ON
(FORWARD operation)Battery voltage
Other than above 0
42 (O/B)Sliding switch ON
(BACKWARD operation)Battery voltage
Other than above 0
PIIA4801E
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Revision: August 20072004 QX56
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and reclining motor LH.
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace reclining motor LH.
NG >> Replace driver seat control unit.
Lifting Motor (Front) Circuit InspectionEIS002YL
1. CHECK FRONT END SEAT LIFTING MECHANISM
Check the following.
Operation malfunction caused by lifter mechanism deformation, pinched harness or other foreign materi-
als
Operation malfunction caused by foreign materials adhered to the lifting motor (front) or lead screws
Operation malfunction and interference with other parts by installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “SEAT LIFTER FR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Lifting motor (front) circuit is OK.
NG >> GO TO 3.
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P336 (Y/G)
GroundReclining switch ON
(FORWARD operation)Battery voltage
Other than above 0
44 (Y/R)Reclining switch ON
(BACKWARD operation)Battery voltage
Other than above 0
PIIA4802E
Test item Description
SEAT
LIFTER FRThe lifting motor (front) is activated by receiving the drive signal.
PIIA0271E
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3. CHECK LIFTING MOTOR (FRONT) CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect driver seat control unit and lifting motor (front).
3. Check continuity between driver seat control unit connector P3 terminals 37, 45 and lifting motor (front)
connector P6 terminals 4, 6.
4. Check continuity between driver seat control unit connector P3
terminals 37, 45 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and lifting motor (front).
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace lifting motor (front).
NG >> Replace driver seat control unit.
Lifting Motor (Rear) Circuit InspectionEIS002YM
1. CHECK REAR SEAT LIFTING MECHANISM
Check the following.
Operation malfunction caused by lifter mechanism deformation or pinched harness or other foreign mate-
rials
Operation malfunction caused by foreign materials adhered to the lifting motor (rear) or lead screws
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.37 (BR) - 6 (BR) : Continuity should exist.
45 (GR) - 4 (GR) : Continuity should exist.
37 (BR) - Ground : Continuity should not exist.
45 (GR) - Ground : Continuity should not exist.
LIIA0698E
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P337 (BR)
GroundLifting switch (front) ON
(DOWN operation)Battery voltage
Other than above 0
45 (GR)Llifting switch (front) ON
(UP operation)Battery voltage
Other than above 0
PIIA4805E
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4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and lifting motor (rear).
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace lifting motor (rear).
NG >> Replace driver seat control unit.
Pedal Adjusting Motor Circuit InspectionEIS002YN
1. CHECK PEDAL ADJUSTING MECHANISM
Check the following.
Operation malfunction caused by pedal adjusting mechanism deformation or pinched harness or other
foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “PEDAL” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Pedal adjusting motor circuit is OK.
NG >> GO TO 3.
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P338 (B/W)
GroundLifting switch (rear) ON
(UP operation)Battery voltage
Other than above 0
39 (Y)Lifting switch (rear) ON
(DOWN operation)Battery voltage
Other than above 0
PIIA4804E
Test item Description
ADJ PEDAL MOTORThe pedal adjusting motor is activated by receiving the
drive signal.
PIIA4555E
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AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
3. CHECK PEDAL ADJUSTING MOTOR CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and pedal adjusting motor.
3. Check continuity between automatic drive positioner control unit connector M34 terminals 37, 45 and
pedal adjusting motor connector E109 terminals 1, 2.
4. Check continuity between automatic drive positioner control unit
connector M34 terminals 37, 45 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK AUTOMATIC DRIVE POSITIONER CONTROL UNIT OUTPUT SIGNAL
1. Connect the automatic drive positioner control unit and pedal adjusting motor.
2. Check voltage between automatic drive positioner control unit
connector and ground.
OK or NG
OK >> Replace pedal adjusting motor.
NG >> Replace automatic drive positioner control unit.
Mirror Motor LH Circuit CheckEIS002YO
1. CHECK DOOR MIRROR LH MECHANISM
Check the following items.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again.37 (G) - 1 (G) : Continuity should exist.
45 (R) - 2 (R) : Continuity should exist.
37 (G) - Ground : Continuity should not exist.
45 (R) - Ground : Continuity should not exist.
LIIA1481E
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
M3437 (G)
GroundPedal adjusting switch
ON
(FORWARD operation)Battery voltage
Other than above 0
45 (R)Pedal adjusting switch
ON
(BACKWARD opera-
tion)Battery voltage
Other than above 0
PIIA4806E
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AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
4. CHECK MIRROR MOTOR SIGNAL
1. Connect door mirror LH.
2. Turn ignition switch to ACC.
3. Check voltage between door mirror LH connector and ground.
OK or NG
OK >> Replace door mirror LH.
NG >> Repair or replace harness.
Mirror Motor RH Circuit CheckEIS002YP
1. CHECK DOOR MIRROR RH MECHANISM
Check the following items.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again.
2. CHECK FUNCTION
With CONSULT–II
Check the operation with “MIRROR MOTOR RH” in the ACTIVE
TEST.
Without CONSULT–II
GO TO 3.
OK or NG
OK >> Mirror motor RH circuit is OK.
NG >> GO TO 3.
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
D41
(R)
GroundWhen motor is
operated UP1.5 - Battery voltage
Other than above 0
2
(BR)When motor is
operated LEFT1.5 - Battery voltage
Other than above 0
3
(O)When motor is
operated DOWN or RIGHT1.5 - Battery voltage
Other than above 0
LIIA1881E
Test item Description
MIRROR MOTOR
RHThe mirror motor RH moves the mirror UP/DOWN and LEFT/
RIGHT by receiving the drive signal.
PIIA0202E
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3. CHECK DOOR MIRROR RH CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and door mirror RH connector.
3. Check continuity between automatic drive positioner control unit connector M33 terminals 14, 15, 30 and
door mirror RH connector D107 terminals 1, 2, 3.
4. Check continuity between automatic drive positioner control unit
connector M33 terminal 14, 15, 30 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK MIRROR MOTOR SIGNAL
1. Connect door mirror RH.
2. Turn ignition switch to ACC.
3. Check voltage between door mirror RH connector and ground.
OK or NG
OK >> Replace door mirror motor RH.
NG >> Repair or replace harness.
Steering Wheel Tilt Circuit InspectionEIS0038L
1. CHECK STEERING WHEEL TILT MECHANISM
Check the following.
Operation malfunction caused by pedal adjusting mechanism deformation or pinched harness or other
foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.14 (GR/R) - 1 (GR/R) : Continuity should exist.
15 (V/R) - 2 (V/R) : Continuity should exist.
30 (Y) - 3 (Y) : Continuity should exist.
14 (GR/R) - Ground : Continuity should not exist.
15 (V/R) - Ground : Continuity should not exist.
30 (Y) - Ground : Continuity should not exist.
LIIA1888E
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
D1071 (GR/R)
GroundMirror motor is operated
UP1.5 - Battery
voltage
Other than above 0
2 (V/R)Mirror motor is operated
LEFT1.5 - Battery
voltage
Other than above 0
3 (Y)Mirror motor is operated
DOWN or RIGHT1.5 - Battery
voltage
Other than above 0
LIIA1889E
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4. CHECK AUTOMATIC DRIVE POSITIONER CONTROL UNIT OUTPUT SIGNAL
1. Connect the automatic drive positioner control unit connector and steering wheel tilt motor.
2. Check voltage between automatic drive positioner control unit
connector and ground.
OK or NG
OK >> Replace steering wheel tilt motor.
NG >> Replace automatic drive positioner control unit.
Sliding Sensor Circuit InspectionEIS002YQ
1. CHECK FUNCTION
With CONSULT-II
Check operation with “SLIDE PULSE” on the DATA MONITOR to make sure the pulse changes.
Without CONSULT-II
1. Turn ignition switch OFF.
2. Check signal between driver seat control unit connector and
ground, with oscilloscope.
OK or NG
OK >> Sliding sensor circuit is OK.
NG >> GO TO 2.
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
M3435 (R)
GroundTilt switch ON
(UP operation)Battery voltage
Other than above 0
42 (V)Tilt switch ON
(DOWN operation)Battery voltage
Other than above 0
LIIA0482E
Monitor item [OPERATION or UNIT] Contents
SLIDE PULSE —The seat sliding position (pulse) judged
from the sliding sensor signal is dis-
played
PIIA4558E
ConnectorTe r m i n a l s
(Wire color)
Condition Signal
(+) (–)
P2 24 (Y/G) GroundSliding
motor
operation
PIIA4556E
PIIA3277E
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Sliding Switch Circuit InspectionEIS002YX
1. CHECK FUNCTION
With CONSULT-II
With “SLIDE SW-FR, SLIDE SW-RR” on the DATA MONITOR, oper-
ate the sliding switch to check ON/OFF operation.
Without CONSULT-II
1. Turn ignition switch OFF.
2. Check voltage between driver seat control unit connector and ground.
OK or NG
OK >> Sliding switch circuit is OK.
NG >> GO TO 2.
2. CHECK SLIDING SWITCH CIRCUIT HARNESS CONTINUITY
1. Disconnect driver seat control unit connector and power seat switch LH connector.
2. Check continuity between driver seat control unit connector P2
terminals 11, 26 and power seat switch LH connector P8 termi-
nals 1, 7.
3. Check continuity between driver seat control unit connector P2
terminals 11, 26 and ground.
OK or NG
OK >> GO TO 3.
NG >> Repair or replace harness.
Monitor item [OPER-
ATION or UNIT]Contents
SLIDE SW–
FR"ON/
OFF"ON / OFF status judged from the sliding switch (FR) sig-
nal is displayed.
SLIDE SW–
RR"ON/
OFF"ON / OFF status judged from the sliding switch (RR) sig-
nal is displayed.
PIIA0313E
ConnectorTe r m i n a l
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P211 (R/B)
GroundSliding switch ON
(BACKWARD oper-
ation)0
Other than above Battery voltage
26 (P/B)Sliding switch ON
(FORWARD opera-
tion)0
Other than above Battery voltage
PIIA4577E
11 (R/B) - 7 (R/B) : Continuity should exist.
26 (P/B) - 1 (P/B) : Continuity should exist.
11 (R/B) - Ground : Continuity should not exist.
26 (P/B) - Ground : Continuity should not exist.
LIIA1125E