Air INFINITI QX56 2004 Factory Service Manual

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SE-46
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and reclining motor LH.
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace reclining motor LH.
NG >> Replace driver seat control unit.
Lifting Motor (Front) Circuit InspectionEIS002YL
1. CHECK FRONT END SEAT LIFTING MECHANISM
Check the following.
Operation malfunction caused by lifter mechanism deformation, pinched harness or other foreign materi-
als
Operation malfunction caused by foreign materials adhered to the lifting motor (front) or lead screws
Operation malfunction and interference with other parts by installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “SEAT LIFTER FR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Lifting motor (front) circuit is OK.
NG >> GO TO 3.
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P336 (Y/G)
GroundReclining switch ON
(FORWARD operation)Battery voltage
Other than above 0
44 (Y/R)Reclining switch ON
(BACKWARD operation)Battery voltage
Other than above 0
PIIA4802E
Test item Description
SEAT
LIFTER FRThe lifting motor (front) is activated by receiving the drive signal.
PIIA0271E

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Revision: August 20072004 QX56
3. CHECK LIFTING MOTOR (FRONT) CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect driver seat control unit and lifting motor (front).
3. Check continuity between driver seat control unit connector P3 terminals 37, 45 and lifting motor (front)
connector P6 terminals 4, 6.
4. Check continuity between driver seat control unit connector P3
terminals 37, 45 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and lifting motor (front).
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace lifting motor (front).
NG >> Replace driver seat control unit.
Lifting Motor (Rear) Circuit InspectionEIS002YM
1. CHECK REAR SEAT LIFTING MECHANISM
Check the following.
Operation malfunction caused by lifter mechanism deformation or pinched harness or other foreign mate-
rials
Operation malfunction caused by foreign materials adhered to the lifting motor (rear) or lead screws
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.37 (BR) - 6 (BR) : Continuity should exist.
45 (GR) - 4 (GR) : Continuity should exist.
37 (BR) - Ground : Continuity should not exist.
45 (GR) - Ground : Continuity should not exist.
LIIA0698E
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P337 (BR)
GroundLifting switch (front) ON
(DOWN operation)Battery voltage
Other than above 0
45 (GR)Llifting switch (front) ON
(UP operation)Battery voltage
Other than above 0
PIIA4805E

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SE-48
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
2. CHECK FUNCTION
With CONSULT-II
Check operation with “SEAT LIFTER RR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Lifting motor (rear) circuit is OK.
NG >> GO TO 3.
3. CHECK LIFTING MOTOR (REAR) CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect driver seat control unit and lifting motor (rear).
3. Check continuity between driver seat control unit connector P3 terminals 38, 39 and lifting motor (rear)
connector P7 terminals 4, 6.
4. Check continuity between driver seat control unit P3 terminals
38, 39 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
Test item Description
SEAT LIFTER
RRThe lifting motor (rear) is activated by receiving the drive signal.
PIIA0274E
38 (B/W) - 6 (B/W) : Continuity should exist.
39 (Y) - 4 (Y) : Continuity should exist.
38 (B/W) - Ground : Continuity should not exist.
39 (Y) - Ground : Continuity should not exist.
LIIA0699E

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Revision: August 20072004 QX56
4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit and lifting motor (rear).
2. Check voltage between driver seat control unit connector and
ground.
OK or NG
OK >> Replace lifting motor (rear).
NG >> Replace driver seat control unit.
Pedal Adjusting Motor Circuit InspectionEIS002YN
1. CHECK PEDAL ADJUSTING MECHANISM
Check the following.
Operation malfunction caused by pedal adjusting mechanism deformation or pinched harness or other
foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “PEDAL” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Pedal adjusting motor circuit is OK.
NG >> GO TO 3.
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
P338 (B/W)
GroundLifting switch (rear) ON
(UP operation)Battery voltage
Other than above 0
39 (Y)Lifting switch (rear) ON
(DOWN operation)Battery voltage
Other than above 0
PIIA4804E
Test item Description
ADJ PEDAL MOTORThe pedal adjusting motor is activated by receiving the
drive signal.
PIIA4555E

Page 2999 of 3371

SE-50
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
3. CHECK PEDAL ADJUSTING MOTOR CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and pedal adjusting motor.
3. Check continuity between automatic drive positioner control unit connector M34 terminals 37, 45 and
pedal adjusting motor connector E109 terminals 1, 2.
4. Check continuity between automatic drive positioner control unit
connector M34 terminals 37, 45 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK AUTOMATIC DRIVE POSITIONER CONTROL UNIT OUTPUT SIGNAL
1. Connect the automatic drive positioner control unit and pedal adjusting motor.
2. Check voltage between automatic drive positioner control unit
connector and ground.
OK or NG
OK >> Replace pedal adjusting motor.
NG >> Replace automatic drive positioner control unit.
Mirror Motor LH Circuit CheckEIS002YO
1. CHECK DOOR MIRROR LH MECHANISM
Check the following items.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again.37 (G) - 1 (G) : Continuity should exist.
45 (R) - 2 (R) : Continuity should exist.
37 (G) - Ground : Continuity should not exist.
45 (R) - Ground : Continuity should not exist.
LIIA1481E
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
M3437 (G)
GroundPedal adjusting switch
ON
(FORWARD operation)Battery voltage
Other than above 0
45 (R)Pedal adjusting switch
ON
(BACKWARD opera-
tion)Battery voltage
Other than above 0
PIIA4806E

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2. CHECK FUNCTION
With CONSULT–II
Check the operation with “MIRROR MOTOR LH” in the ACTIVE
TEST.
Without CONSULT–II
GO TO 3.
OK or NG
OK >> Mirror motor LH circuit is OK.
NG >> GO TO 3.
3. CHECK DOOR MIRROR MOTOR LH CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and door mirror LH.
3. Check continuity between automatic drive positioner control unit connector M33 terminals 16, 31, 32 and
door mirror LH connector D4 terminals 1, 2, 3.
4. Check continuity between automatic drive positioner control unit
connector M41 terminal 16, 31, 32 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
Test item Description
MIRROR MOTOR
LHThe mirror motor LH moves the mirror UP/DOWN and LEFT/
RIGHT by receiving the drive signal.
PIIA4784E
16 (O) - 3 (O) : Continuity should exist.
31 (R) - 1 (R) : Continuity should exist.
32 (BR) - 2 (BR) : Continuity should exist.
16 (O) - Ground : Continuity should not exist.
31 (R) - Ground : Continuity should not exist.
32 (BR) - Ground : Continuity should not exist.
LIIA1880E

Page 3001 of 3371

SE-52
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
4. CHECK MIRROR MOTOR SIGNAL
1. Connect door mirror LH.
2. Turn ignition switch to ACC.
3. Check voltage between door mirror LH connector and ground.
OK or NG
OK >> Replace door mirror LH.
NG >> Repair or replace harness.
Mirror Motor RH Circuit CheckEIS002YP
1. CHECK DOOR MIRROR RH MECHANISM
Check the following items.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again.
2. CHECK FUNCTION
With CONSULT–II
Check the operation with “MIRROR MOTOR RH” in the ACTIVE
TEST.
Without CONSULT–II
GO TO 3.
OK or NG
OK >> Mirror motor RH circuit is OK.
NG >> GO TO 3.
ConnectorTe r m i n a l s
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
D41
(R)
GroundWhen motor is
operated UP1.5 - Battery voltage
Other than above 0
2
(BR)When motor is
operated LEFT1.5 - Battery voltage
Other than above 0
3
(O)When motor is
operated DOWN or RIGHT1.5 - Battery voltage
Other than above 0
LIIA1881E
Test item Description
MIRROR MOTOR
RHThe mirror motor RH moves the mirror UP/DOWN and LEFT/
RIGHT by receiving the drive signal.
PIIA0202E

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AUTOMATIC DRIVE POSITIONER
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Revision: August 20072004 QX56
3. CHECK DOOR MIRROR RH CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and door mirror RH connector.
3. Check continuity between automatic drive positioner control unit connector M33 terminals 14, 15, 30 and
door mirror RH connector D107 terminals 1, 2, 3.
4. Check continuity between automatic drive positioner control unit
connector M33 terminal 14, 15, 30 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
4. CHECK MIRROR MOTOR SIGNAL
1. Connect door mirror RH.
2. Turn ignition switch to ACC.
3. Check voltage between door mirror RH connector and ground.
OK or NG
OK >> Replace door mirror motor RH.
NG >> Repair or replace harness.
Steering Wheel Tilt Circuit InspectionEIS0038L
1. CHECK STEERING WHEEL TILT MECHANISM
Check the following.
Operation malfunction caused by pedal adjusting mechanism deformation or pinched harness or other
foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.14 (GR/R) - 1 (GR/R) : Continuity should exist.
15 (V/R) - 2 (V/R) : Continuity should exist.
30 (Y) - 3 (Y) : Continuity should exist.
14 (GR/R) - Ground : Continuity should not exist.
15 (V/R) - Ground : Continuity should not exist.
30 (Y) - Ground : Continuity should not exist.
LIIA1888E
ConnectorTerminals
(Wire color)
ConditionVoltage (V)
(Approx.)
(+) (–)
D1071 (GR/R)
GroundMirror motor is operated
UP1.5 - Battery
voltage
Other than above 0
2 (V/R)Mirror motor is operated
LEFT1.5 - Battery
voltage
Other than above 0
3 (Y)Mirror motor is operated
DOWN or RIGHT1.5 - Battery
voltage
Other than above 0
LIIA1889E

Page 3003 of 3371

SE-54
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
2. CHECK FUNCTION
With CONSULT-II
Check operation with “TILT MOTOR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Steering wheel tilt motor circuit is OK.
NG >> GO TO 3.
3. CHECK STEERING WHEEL MOTOR HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and steering wheel tilt motor.
3. Check continuity between automatic drive positioner control unit connector M34 terminals 35, 42 and
steering wheel tilt motor connector M68 terminals 1, 5.
4. Check continuity between automatic drive positioner control unit
connector M34 terminals 35, 42 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness.
Test item Description
TILT MOTOR The pedal adjust motor is activated by receiving the drive signal.
PIIA0280E
35 (R) - 1 (R) : Continuity should exist.
42 (V) - 5 (V) : Continuity should exist.
35 (R) - Ground : Continuity should not exist.
42 (V) - Ground : Continuity should not exist.
LIIA1431E

Page 3005 of 3371

SE-56
AUTOMATIC DRIVE POSITIONER
Revision: August 20072004 QX56
2. CHECK SLIDING MOTOR SENSOR CIRCUIT HARNESS CONTINUITY
1. Disconnect driver seat control unit connector and sliding motor LH connector.
2. Check continuity between driver seat control unit connector P2
terminals 16, 24, 31 and sliding motor P4 terminals 1, 2, 3.
3. Check continuity between driver seat control unit P2 terminals
16, 24, 31 and ground.
OK or NG
OK >> Replace sliding motor.
NG >> Repair or replace harness.
Reclining Sensor Circuit InspectionEIS002YR
1. CHECK FUNCTION
With CONSULT-II
Check operation with “RECLN PULSE” on the DATA MONITOR to make sure the pulse changes.
Without CONSULT-II
1. Turn ignition switch OFF.
2. Check signal between driver seat control unit connector and
ground, with oscilloscope.
OK or NG
OK >> Reclining sensor circuit is OK.
NG >> GO TO 2.16 (W) - 3 (W) : Continuity should exist.
24 (Y/G) - 2 (Y/G) : Continuity should exist.
31 (L/Y) - 1 (L/Y) : Continuity should exist.
16 (W) - Ground : Continuity should not exist.
24 (Y/G) - Ground : Continuity should not exist.
31 (L/Y) - Ground : Continuity should not exist.
LIIA0706E
Monitor item [POERATION or UNIT] Contents
RECLN PULSE —The seat reclining position (pulse) judged
from the reclining sensor is displayed
PIIA4558E
ConnectorTe r m i n a l s
(Wire color)
Condition Signal
(+) (–)
P2 9 (L/R) GroundReclining
motor
operation
PIIA4559E
PIIA3278E

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